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Showing content with the highest reputation on 01/03/21 in Posts

  1. Made some more progress today, gave it an eyed up wheel alignment, fitted up the new booster and master cylinder, repinned all the door hinges, refitted the cert plate and cut off the old exhaust ends. Also pulled out the pedal box to give that a small birthday while it was easy to get to it. Back on its own 4 wheels for the first time in 9 months.
    20 points
  2. Seam sealed beneath and in the trunk. Undersealed over the seam sealer beneath. And while waiting for that to dry etc. I made a start on mounting the 50s chevy pickup wipers. Work well and much easier to purchase than the sedan's cable driven factory units. Then made a start on connecting them to the cut down lexus wiper motor. Is working Well. Even has an extra motor to park the wipers. Which should bring them to a rest on the windscreen rubbers very nicely. Will continue once Ulrich is back open again. So I can replace the wood. Today I reassembled the rear subframe and reinstalled.
    11 points
  3. After 2 hours on the rotisserie and the internal temp to just over 60 I took it off, wrapped it and let it rest for about 20mins. Removed the string and cut it up and damn, not too bad. Juicy and tasty as, sticky on the outside. Made a quick sandwich for a snack and will be using it in noodles tonight. Probably freeze some of it for future ramen.
    10 points
  4. Got the sump inner core pattern assembled and painted. Should be a lot easier to sand than the outer pattern! This gives a visual on what its making. The main inner core. A couple of smaller cores attach to it.
    9 points
  5. Building the 1961 Datsun 310 Bluebird - RHS Outer Sill Weld Together and Details. Time for an update reporting progress on the RHS build. Outer sill segments are welded together, including most details; end stub, end stub cap and inward joggle at B-post base. Lower A-post below the belt line and down to the sill (about 2 feet w/hinge mount points) is fabricated, tack welded together and temporarily fitted (mock up installed with Teks). The Inner body skin behind the A-post is repaired with another patch. The RHS front door hinges are rebuilt. Both RHS doors were dragged out of the backyard shed, temporarily installed and checked for fitment with the other repairs and all is well. The lower half B-post repairs are underway and nearly complete. Posting the outer sill progress/pics. Other stuff noted above to follow later. The three RHS outer sill segments welded together. Fully welded on both sides since outer is to be sanded flush. Trimmed and fit checked. Kept the weld heat under control by alternating tacks between the different joints and sides and it all came out exceptionally straight. It could have easily warped and created a nightmare. I don't recommend this approach but with a cheap 18 inch metal folder it was the only way to make it. Looks good enough now to proceed with the forward end stub. Next, making the RHS outer sill forward end stub. What follows is the detail required to allow the sill to have clearance with and tuck under the inner front fender support structure. I had no reliable original stub to copy from and just made my best guess to reverse engineer this new stub from the mutilated mess of the original as shown in the pics below. I got lucky and it does test fit snugly with the inner fender structure with just a millimeter or two of clearance. Then, after dressing the stub welds, I made a forward end cap to fit it based on best guesstimate. Stuck it together using a resistance spot welder from Harbor Freight. First time use where I may have been holding the dwell a bit too long. It's permanently stuck on at any rate. In preparing for future repairs and fitment work on the B-post, I made a cutout about mid-length down the outer sill to fit the base, same as on the original. Then filled it in with a custom small inward joggle piece that, though small, took several hours to build. Tacked it in and left it that way for now until the B-post is complete and fit is assured. Made several other minor joggles along the pinch weld flanges to accommodate overlap of bracket flanges and such. Not worthy of pics. That's it for this post on the RHS outer sill. As mentioned in the beginning of the post, hopefully more to follow soon. Discussion: https://oldschool.co.nz/index.php?/topic/60267-marts-pl310-61-datsun-bluebird-sedan/ Build: https://oldschool.co.nz/index.php?/topic/60264-marts-pl310-61-datsun-bluebird-sedan/
    7 points
  6. So we did a few things in between family obligations. We replaced the oil and oil filter - well partner did, I remain an oil change virgin. Not too much mess, at least nothing a rag and some dirt won't clean up! We found top dead sexy and got the distributor installed - 50% chance it's right, gotta figure out if it's on the compression stroke but #1 cylinder is too hard to reach rn - we'll find a cork or something. We also dropped the dizzy nut and it entered a portal to another dimension. So now a windscreen wiper needs a new nut. We followed this guide and so have the timing 10 units before TDC. Pulled all the spark plugs to check them out, visual inspection seems good even if they're two different brands for some reason. Metal isn't bent, can't measure gap but it seems okay, no crazy build up of stuff, threads are dry (ignoring penetrating lube), except... ... #3 is cross threaded >.< It took most of my strength w/ a breaker bar to get out and required the use of the bar for almost the entire journey out. It's definitely the socket that is the main problem as other spark plugs struggled to go back in too. The socket itself looks like it has some crap in it - I got a pokey magnet in there and drew out a fairly substantial amount of shavings and dust from the threads, but... eek. Down the line we'll try a back tap and see if we can avoid removing the head. We're still lacking the dizzy cap (on its way) but we hooked all the bits back up and the battery and tried to turn it over just to see if that was all good - but nothing, just a click. Full charge on the battery with plenty of CC's tasting like these. The click doesn't seem to come from the starter but rather inside the car on the passenger side which is confusing, but the day was long so we called it there. To do: figure out exactly what's making the noise, also remove starter and see what it looks like / poke it with some electricity. ---- Bonus older gif: pop pop up and down headlights! The left hand horn likes to sound when the lights pop up. I'm guessing there's a short somewhere. The left light also is sliiightly slower to come up giving it a lazy eye effect. Features?
    7 points
  7. Pulled the engine out of the falcon and got all the turbo goodies bolted up, been setting up the ECU to take the Fg throttle and injectors and converting the tune file with HP tuners while on nightshift, should have the engine wiring finished off in the next day or 2. Getting rid of the falcon body soon so will get the wagon back on the hoist and look at getting the engine in and mounted
    6 points
  8. We've got some mates coming around tonight so decided that we'll make some Soba noodles, and thought about doing some chashu pork on the rotisserie to break it in. Picked up about a kg worth of pork belly, had a crack at rolling and tying it up (one end had more meat than the other and I didn't want to trim it). I salted the meat and let it sit for about an hour. After I made a Japanese style marinade using soy (light and dark), mirin , sake, rice wine vinegar, sesame seeds, garlic and ginger. Let it marinade in that for about an hour and a half then setup the bbq. It's been on for about 45minutes since that last pic and tbh it probably doesn't need too much more. Will keep you guys posted shortly.
    5 points
  9. Changed out the cluster to the one from the old van so I've gained a tach, 100,000 less kms and 20 km/h more top speed ..haha, mucked around with the wiring, I'm not so good at it but I guess simple 80s wirings not too bad... looks better nice labelling still managed to get a wire wrong though :/ blew up my alternator somewhere along the way, so I got a spare nissan skyline one and swapped the center out to the silvia housing (housings are different)
    4 points
  10. Brought these from jaycar. They work amazing!! Only $20, super happy with them. Im sure there's much better ones, but even on insulated connections they make an unbelievable tight grip. Wish I'd had these years ago. I have 4 other sets of crimping tools...they're all just rubbish compared to this.
    4 points
  11. Today I made a start on tidying up some of the loose engine parts. De-greased the tappet cover and sump and then took to them with a wire wheel. Chucked a few coats of satin black engine enamel on the tappet cover and it came up mint. The indentations on the sump need a bit more work before its ready for paint so I'll carry on with that tomorrow.
    4 points
  12. Cut out the rust. Stole a bit from the other car. Then spent what must have been HOURS getting it to fit properly. I did minimal linishing at the back because it's hidden behind the dash. Then I cut out a new bit for the front and spent another age getting it to fit.
    4 points
  13. Fuck I hope I don't ever need to remove this.
    4 points
  14. Altenator works now, I've now got all the dash functions I need, should get some 100amp fuses for battery though as the loom never had them ?? Would explain the altenator
    3 points
  15. Waiting on a couple of seals and a number plate light, but this is about ready to get inspected
    3 points
  16. I mounted that expansion tank somewhere convenient. Went for a drive and all seems to be behaving. I also made some racks to carry long things, did the rear a few days ago and sorted the front out today. I'll get those zinc arc sprayed I imagine; Might make the rear clamp on rather than ratcheted, you have to properly crank it up to prevent it from rocking a little....
    3 points
  17. So yeah, after googling what wear rings are supposed to look like, and frowning at the pump from the donor banana ski, yesterday I removed the pump from GreenWaste and had a look. Two pumps on the floor, pretty much identical. IMG_20201231_102856_1 by John Bell, on Flickr I believe this is what a bad condition wear ring looks like, from the donor ski. Cracks and grooves, not toight. IMG_20201231_113413 by John Bell, on Flickr And this is what the Greenboat had in it, note the missing material around most of the diameter. Lots of clearance. IMG_20201231_113456 by John Bell, on Flickr So I figured bad was better than worse than bad, so gooped it up and bolted it back on. IMG_20201231_121347 by John Bell, on Flickr Sploot. IMG_20201231_133309_1 by John Bell, on Flickr Launched it into the harbour this morning and pootled about with VG and Keltik, it still doesn't feel 100%, but its pretty usable now and hooks up and pisses off quick enough for me. I will likely order some bits and pieces to tidy up the original pump and probably swap it back in the winter perhaps. IMG_20210101_104035_1 by John Bell, on Flickr I'm waiting for a China GPS speedo, and need to fit a hour meter/tacho, fit some latches to the hood, attach the paddles in a better way, and I think that'll do for now. What a novelty having a working toy
    3 points
  18. Well after staring at this in the workshop for the last 3 months while we've been massively busy at work and I've been caught up on the weekends entertaining my son I finally managed to get a couple of days to spend on this so I managed to mount my seats and get my tunnel fab'd up. I had to change my plan for the seats as my original design ended up too low and too far back surprisingly. Also the cert man wasn't happy with me removing the stiffer running the width of the car. So, I went back to the drawing board and came with this Then I made up a cardboard gearbox tunnel. And decided I better turn it into steel Happy to have those big jobs ticked off. I do still have to pull the engine and box to weld underneath but the hard work is done for the tunnel fabrication which is great
    3 points
  19. today went better. i got the little bit of surface rust of the inside of the scuttle panel and chucked some brunnox on it. poured some brunnox inside the fuel filler flap and then chucked some primer on things. yesterday i primed the car again so only the drivers side needs another coat, the rest of the car is ready for wet sanding. yay, wet sanding. 2020-12-30_02-33-07 by sheepers, on Flickr 2020-12-30_02-32-59 by sheepers, on Flickr 2020-12-30_02-32-45 by sheepers, on Flickr 2020-12-30_02-32-52 by sheepers, on Flickr before priming, 2020-12-30_02-33-43 by sheepers, on Flickr 2020-12-30_02-33-36 by sheepers, on Flickr after priming, 2020-12-30_02-33-29 by sheepers, on Flickr 2020-12-30_02-33-22 by sheepers, on Flickr
    3 points
  20. Since I can only safely mix 30kg of sand at once Ive made some partitions over the pattern for 30kg sections. Will do some sequence of removing walls and work along the pattern. Probably key the sand together as I go so hopefully it doesnt shift around. The base is an overly complicated 30mm spacer that the inner cores align to. Could have done it out of wood but when you have a big printer why not! Once Ive figured out if the pattern works I will be able to fill it at the foundry in one go without partitions.
    3 points
  21. Time to chuck up a post about my latest project since iv just started pulling apart the donor car, starting with 1 VR commodore wagon the old 3.8s rod came knocking and put a window in the block. Iv stripped the interior of that, to make way for a 6 point sfi cage and rear tubs to the rails to accommodate wider rubber and a parallel 4 link 9", to be commenced early/mid 2021, Now the fun part the bf falcon some of you may know from such shenanigans as palmy/fielding 2020 swapmeet is giving up its engine for the repower to be backed up by a th400, now let's see what the stocker na can do with an FG xr6 gt3576 strapped to the side of it. Already got some goodies a powertune digi dash to run off the factory ford pcm and eventually the link g4 when it goes full send, also picked up an e boost2 to keep the boost pixies under control. Plan is to make it fully street legal and be able to swap wheels and tyres and go full send on the drag strip/power cruise and chrome.
    2 points
  22. Get us one of these please love - this ones fucked. Previous owner has indeed filled the seal lubrication hole with silicone. Everything has also been reassembled less the electrical insulation stuff so the front bearing was pretty loose in the outer housing - had not been loctited into place as they recommend. Might need to get someone talented on a lathe to spin up a new spacer. This ones got a pretty decent groove in it from the oil seal and the front edge is also chooched so i cant just turn it round. I really hope its not part of the shaft! I guess I'll find out soon enough once I get a suitable sized puller to go in there.
    2 points
  23. ^ I remember how amazing yet horrible that was. said dumb shit, complete with youtube clickbait. if tldw. it almost gained 1kw. so success ? just need one of these
    2 points
  24. GPS plotted a path of some of our journey yesterday. Stupid tide running away from us though, there only seems to be a couple hour window where you have useable water depth. boat journey 2-1-21 by John Bell, on Flickr
    2 points
  25. Yip, thats how I was feeling as I figured out that a lot the wires are spliced and share common power/earths etc. But by testing the resistance (ohms) through each circuit using a multimeter, i got there in the end. Pretty common shit I guess...but for an electrically retarded person like myself, self teaching as I go along, its a lot of condensed learning to fit into my already closed mind. That said, I'm there now. Each wire labeled and each corresponding circuit tested and working via its switch. so I'm now ready to buy expensive tools to strip and crimp the wires and then try installing OEM style connectors, yet another thing I've never done...but will soon have to figure out quick smart If I want it to work.
    2 points
  26. I always knew this topic would end up at the holy grail, the su carb
    2 points
  27. Next video will have dumb shit
    2 points
  28. Its alive! Idles, revs and has oil pressure (the light turns off) and fuel level sender , as you can see not much else but a good sign I haven't shorted stuff out or done something wrong, now it's just tidy tidy everything, happy new years!
    2 points
  29. Got the body in primer about 6 weeks ago It then took me all that time to get it up to a reasonable state so that it could then be painted. So then a couple days a go we loaded it up on the trailer (only just fit!) and dragged it into the spray booth at work. Sprayed the base and clearcoat on, it turned out pretty good! A few runs around in places, but nothing that can't be fixed. Pretty stocked really! Could of easily gone wrong haha. Gonna leave it in the booth for a few more days to harden, then take it home and get some underseal on the underside. In the meantime get the rest of the panels ready for some paint too.
    2 points
  30. Burn off the other night went well. Got it to 500f and it held there for atleast 3 hours without adding any extra fuel. Left it going when I went to bed. Had a look in the morning and it looked like this... Emptied out the ash and gave it a good clean to prep it for seasoning and paint. Just used olive oil on the inside as that's all I had and Mangawhai shops are shit to go to this time of the year cause of all the jafas and northern bass homies.
    2 points
  31. So yeah, as seen above, took it back to the water yesterday and it does run a lot better when its not breathing its own fart cloud. Picture of failed engine mount and V band that needed toightening. IMG_20201228_170634 by John Bell, on Flickr I'm not completely happy with its performance though now its making full more power, it doesn't 'bite' the water like I would expect, if you feed it more power than it can shift water, it nangs out and feels slower than if you were to nurse it up to speed. You can see/hear this in one of the vids. It handles a quite loosely, but I don't have much reference to compare it to, aside from the donor ski which carved corners like a water-skiing cut cat, comparatively. If you do manoeuvres that are too aggressive or any spins it comes off the plane pretty easily and doesn't pop out of the water like the motor seems capable. So next step is to look at the spare jetunit, if its any better pop it on for testing, and I feel I'll probably wind up giving one of the pumps a birthday. Cute IMG_20201228_182945 by John Bell, on Flickr
    2 points
  32. Cut up some thicccc expanded mesh(this shit is about 10x6mm thick and expensive as shit. We use it for guarding heavy machinery, luckily we had some left over for the coal rack and also for the grille. And here's the upper vent mocked up. These are called butterfly vents and are used for marine purposes. Took me bloody ages to find something like this
    2 points
  33. Bushes replaced and the Valiant drives nicely again. One of my boys finished year 8 schooling, they have a formal and parents etc are invited to drop their kids off at in front of the school hall pre formal. The valiant beached quite loudly as I was turning onto the field which my son thought was fantastic. Good boy! He was very keen on some school field paddock work. I exercised the utmost restraint and no circles were done. Here's a pic of some previous grass silliness. I put the Superlites on for the school run. Then decided I didn't like them and took them off the next day. I'd quite like a set of these modernized Cheviot Quattro's but the budget won't stretch that far at the moment. anyway that's enough sharnes. I have done some productive stuff too. I got my big fuel tank re tested, blasted and painted. It's slightly larger in diameter and considerably longer than the old one. My calculations suggest it will hold about 20 Liters more fuel than previous which equates to about %30 more. Luckily I managed to fit it into the old tank straps which was a bonus and saved much fucking about. Old. New. I Need to sort out some new ducting as the tank has is designed for 60mm as opposed to 2 inch as before and I'll be ready to run. This tank has a little magnetic gauge sender unit that is miles different resistances to what the factory sender had. It looks fairly simple and I'd like to see about getting it changed so I can use my factory gauge. Has any one in ChCh delt with E Parrot and Sons since it has changed hands? Are Robinson instruments still around? Suggestions please.
    2 points
  34. And some photos to stick on the fridge
    2 points
  35. I'm pleased to announce this boat has successfully completed stringent reliability and performance trials including but not limited to... Shallow water performance Low speed maneuverability Higher speed spins and dicking around
    2 points
  36. Finished up the bumper mounting brackets. 5x large plug welds down through the floor skins into them. Outer edge also has a strap on each side, which it is also plug welded through. Also filled the last of the holes in the sills. Have now painted a chassis black primer underneath, anywhere underseal did not exist. Seam sealer tomorrow. Then spray on underseal.
    2 points
  37. Have all the interior door handles back on. Modified the rods and clips from the Lexus doors. To join the Chevy Handle mechanisms to the Dakota Digital Bear Claw Latches. I had to modify/weld the lever on the Dakota Digital bear claw, so it would pull forward/Back, instead of Up/down. And had to cut the existing holes in the door a little bigger. They work beautiful and reliably so far. Latch smoothly. And have a good amount of movement in the handle, before they release the doors. Next up was the brackets for the rear bumper. Folded up a couple of 50x5mm steel brackets to bolt onto existing m12 holes. Couple more to make for the front of the bumper irons. Then all will be spot welded through the double skin beam in the floor, that the factory tow bar and hooks is mounted to.
    2 points
  38. Project discussion: I bought this site unseen from Hamilton a few months ago. It's @brocky41 old car credit to him getting it going. Turns out it's actually a good thing... Spend the last little while fixing little stuff.. Tuning it up and charging around the country side. Really nice jap cruiser.
    1 point
  39. Pull the relay out and see if you can pop the cover off and inspect the contacts. Maybe use a multi meter to check that the relay is doing its relay-ing. Also, inspect any electtrical boards in the machine for obvious faults. Capacitor popped open, or burnt component, that kinda thing
    1 point
  40. check the fuse? i think the low power and high power circuits are seperate
    1 point
  41. Brought these today. They work amazing!! Only $20 from jaycar, super happy with them.
    1 point
  42. Sorry to go off topic valiant, but piazzanoob have u had much experience with these ICE systems on 440s? Would like to chat to u regarding the timing curve details etc if poss. Im a little uncertain where to set mine with the cam in mind. Cheers Shane
    1 point
  43. Just look at the difference... I am fully stoked - updated 29th December with latest photo to show actual engine bay comparison with subframe etc installed Before During After
    1 point
  44. Petone Radiators do chemical cleaning on fuel tanks, weren't super spendy from memory. Drop it off, pick it up, zero fucking around with trying to get chain/nuts out again.
    1 point
  45. Between filling the intake grate with lake weed, and intermittently running like a bag of dicks, it was a bit lame initially. It would start off strong but get to the point where you got 100% power or a stumbling surging 20%, but run progressively worse the longer you persevered. When it went well it'd skim along pretty well with two of us in it. IMG_20201219_155248 by John Bell, on Flickr IMG_20201219_155144 by John Bell, on Flickr
    1 point
  46. Started on the tunnel and finally got some trim parts painted!
    1 point
  47. Building the 1961 Datsun 310 Bluebird Floorpan - Trimming the perimeter. Started off by taping together a big piece of cardboard. Then carefully trimmed it to fit between the inner sill, toe board, tunnel and rear seat box. Added extra margin with heavy paper to the edge. This was laid into the floorpan. Then I pie cut and panel beat the mating trans/drive tunnel edges to merge in accordance with the cardboard/paper template. The other edges were bent similar but with less beating since no blend radii were required. The result. First of dozens of fit checks in car. It looks not too bad for a start. It's a lot better than the rusted out floor that was there. Visible progress finally! I left it this way for a long while since the excess material made it a bit easier to grasp the floorpan by the edges and pull it out after each fit check. Much later, after doing several other feature additions, bend/panel beat tweaks, and satisfied the trim edge plans were stable and would work, I taped and trimmed all the finalized edges, then applied an angle grinder cut-off wheel and tin snips. Trimmed. Next up is duplicating factory body mount indentations and other stiffening features. Still lots more to catch up on. Might take me the rest of the day to upload it all. More posts soon… Discussion:
    1 point
  48. Building the 1961 Datsun 310 Bluebird Floorpan - Details. I have a large number of photos and so I'll split this update into several posts to minimize any load delay. Picking up the story from mid-August 2019, beginning with making underfloor bracket replacements. The first of two bracket replacements, all the others were salvaged from the existing floor. This first bracket is simple, but I had destroyed the original by cutting off the flange that attaches it to the inner sill. I just sketched up the right side bracket while laying under the car. Left floor bracket has the flanges bent in the opposite direction from the sketch. The second bracket that needed replacing. The underfloor support, inner attach for the lift jack pipe and parking brake lever attachment. It appears to have been destroyed by road debris that was run over by a previous owner. My guess is piece of rebar hit at 60 mph by the front tire that was kicked up and pierced the underside. The damage included a hole in the floor and a severely bent steel shaft for the parking brake. I split it in half for measurements since that's that way I'll make a replacement and then weld it into one. It includes minor complications to be duplicated such as the gusset bumps and welded on 5/16 - 24 fine thread square nuts (which are hard to find in 24 pitch thread btw). Made the halves out of 1.5 mil. Initial checks against the inner sill. Making parts and finishing up the welds. Then I welded on the square nuts, fuel line clip and forged the four gussets into the corners with 3/8 inch rod, some heat from a MAP torch, and backed up with angle iron. The hole in the middle is where it will get pinned to the lift jack pipe. Nissan had brazed the original attachment to the pipe sides but that's not practical for me since I'm welding this to the floor first and attaching to the pipe last. The heavy oxidation was later cleaned off with a soaking in muriatic (hydrochloric) acid. Additional posts soon... Discussion:
    1 point
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