Popular Post d.p.n.s Posted May 1 Author Popular Post Report Share Posted May 1 another picture less update sorry.. we had another play with things on Saturday.. wasn't getting anywhere again... we stopped went through it all again and again.... and then Simon said ...what about the plugs ? I told him they were new last weekend..so we thought fuck it ... I grabbed a set of old shitty plugs (pretty sure they came out of the motor in the old rusty wagon).... we slapped them in and she fired up.... only for a few seconds but she fired up... I can't tell you the feelings I had when she started..... just gave me instant hope that I had done things right ....was like a massive weight of my shoulders.... still heaps to do but I know now it will work.. massive thanks to @Stufor the basic tune to make it run.... cheers. 11 Quote Link to comment Share on other sites More sharing options...
Popular Post d.p.n.s Posted May 7 Author Popular Post Report Share Posted May 7 had a wee play today.. moved the trigger 2 wheel around a bit so it's not to close to the crank trigger missing tooth. put some new plugs in gapped to 25tho. change a setting on the injector fuel main from sequential to batch fired...(after reading up a bit more the 36-1 on trigger 2 is a bad fay of doing it.. it just needs to be 1 tooth and that will help it sync better) ..so ill pull the pulley off and cut all the teeth off apart from one and put it all back together and try and get sequential injection to work..... but hay in the mean time this happened 11 1 Quote Link to comment Share on other sites More sharing options...
d.p.n.s Posted May 8 Author Report Share Posted May 8 pulled the crank and cam triggers off.. from what I've read and other have confirmed the 36-1 trigger is really hard to sync with a 36-1 crank trigger... so the car runs and even if I unplug the cam sensor it still runs as the injectors are being group fired.. but I want sequential so the answer is to have just 1 tooth on the cam trigger .... so I'm just going to cut another 34 teeth of yhe wheel and go with that.. once I have the rigger sorted and the intercooler piping (ordered today) in place then I'll be able to start tuning it properly... but she runs.... huge weight of my shoulders. 7 Quote Link to comment Share on other sites More sharing options...
Popular Post d.p.n.s Posted May 9 Author Popular Post Report Share Posted May 9 well I cut all the bar 1 tooth of the cam sensor..changed trigger 2 sync mode to CAM PULSE WINDOW and then just set that to 50° and she's now running both DRIECT SPARK and SEQUENTIAL INJECTION. she basically a modern engine now with classic pinto oil leeks.. haha not much else I can do till I make intercooler piping (and our postal service dictates when I get the stuff)... but even at idle the air coming out of the turbo is pretty significant. also set the water pump temp to 70° .. engine temp got up to 68° water pump kicked in...temp got to 71° fan kicked in and bought temp down to 65° in no time.... so I'm happy with the coolant system. RX2 70mm thick radiator, 14" fan in shroud ,electric waterpimp... on a side note ... heater was awesome within minutes. cheers 17 Quote Link to comment Share on other sites More sharing options...
d.p.n.s Posted May 14 Author Report Share Posted May 14 had bits turn up for the intercooler piping.. just had to male a flange and weld the piping where I needed it from the turbo outlet. so apart from the speedo cable and hose for overflow tank that's everything that needs to go in the engine bay......its bloody busy in there now. was doing a wee bit of tuning today and getting the motor upto temp .. then when I shut it off and had lunch.. come back in the garage and found this so it looks like the motor is coming before tuning now.. I'm not sure if it's anything major or just some leaks... the motor is an unknown and didn't cost me much $$$$$ it was only to get it all set up and tuned .. put I'll pull it and see what's what and go from there. 4 Quote Link to comment Share on other sites More sharing options...
d.p.n.s Posted May 15 Author Report Share Posted May 15 took a couple of hours ...but the motor ame out.. not all that hard and mostly complete. there are a few things...leaking. *both sump and rocker gaskets are weeping ..(rear of the sump seems pretty bad)( left rear of the rocker cover is pretty bad.)...may be another reason for the sump gasket ....get to that later. I did put a full gasket set through it in October 2020 but it's sat dry till about a month ago. *the clamp on the oil return had had slipped down and so had the hose and kinked it a bit (not sure if it's enough to stop oil flowing..maybe another reason for that ...) also might need a restrictor in the oil feed line *oil on the block from the crank breather (may be another issue causing that ) .. * the main thing is I lost about a litre + on the floor..the oil cool and lines were full... and I only put 4l in.... and drained 5 out...that smelt a lot like fuel... so I think the 1st few days of fucking around with ecu setup ..it pumped so much fuel into it that it filled the sump... enough for the gasket to leak....the turbo drain to be blocked .. so replace a few gaskets and try again... there are a few things I wanted to do anyway and would have been easier the motor out... so 2 birds 1 stone. 6 Quote Link to comment Share on other sites More sharing options...
d.p.n.s Posted May 16 Author Report Share Posted May 16 pulled the sump off ...found *gasket was fucked .. *sump was full of crap (petrol must have cleaned the motor as I cleaned the sump last time I had it apart). *motor is clean...oil pick up is clean . *sump.must have been full as there was what looks like airated oil up the front of the sump (not bowl) from where it was churned up by the crank... 4x800cc injectors may have filled the bores on a few occasions. *pulled a main cap (didn't get a pic ) pulled a couple of big end caps and they seem ok. also found oil in the bellhousing and you can see a stain on the steering shaft and oil on that side ... so I'm going to say 90% of it came from seal letting go at the rear and oil coming out the turbo drain. so on conclusion.....slap a new sump gasket in ,, a new rocker cover gasket and go again... lol got a few other things to do while it's out .. 9 Quote Link to comment Share on other sites More sharing options...
d.p.n.s Posted May 17 Author Report Share Posted May 17 few .ore bits done.. *battary box mounted ,factory jack and a wheel brace and boot cleaned. *passenger door on , door card cleaned and also put on door (need to find a set of oldschool-ish speaker covers to cover the holes). *sump back on motor with new gasket.. *new oil Drain from turbo done. *tightened all the bolts around the turbo I struggling get up with motor in the car. *made the block breather fit better and now it sealed *put a bracket on for the dipstick tube. *pulled the coolant temp sensor out of the ba k of the head and put a new frost plug in... it was a good idea but a pain in the arse ti get to and when I pulled it out you could see it was starting to weep any way.... Could find anywhere to put the temp sensore other than where tha bung is at the rear of the exhaust side of the block..(will need a small heat shel).. I no its not ideal to have ut in the ocean and head is best ... but it's not really doing much ..the electric water pump has its own temp sensor in the top rad hose and that controls pump and fan (takes care of all the cooling ). 5 Quote Link to comment Share on other sites More sharing options...
d.p.n.s Posted Monday at 09:22 Author Report Share Posted Monday at 09:22 git a few bits done while engine was out... new rocker cover gasket .. some P clips to hold oil feed for turbo out the way small heat sheld to help keep the heat away from the coolant temp sensor I moved to the black. made a small sheld to keep heater hoses out the way and tucked back on the firewall has a small vibration in the steering system.. turnout being the Bush that sit in the fire wall and the column slides through it.. ended up being a ass of a job. got the motor all back in.. nice to know she comes out and in ....with little hassle extended the temp sensor wires moved the mountings on the heat sheld... gave me a wee bit more room around the manifold hoses tucked out the way back on the wheels.. now. I also removed the oilcooler setup as the oil light would flicker so I wonder if it was low on pressure because of the cooler.. I'll grab some new oil and filter this week and then hopefully get back to tuning on Saturday....if the motor holds up. .I dug the drivers door out and ut seems in bloody good condition.. just missing chrome surrounds (think I have a set ). and missing door handle ..found the one from the rusty old wagon but uts broke.. (might have ti steel it from the white mk3 for now) on a side note ... about 5 months ago I ordered some LS1 coil boots and terminals.... but actually gave up on them ever getting here.. and just made them out of the ones I had .. but they arrived today.. so may about better terminals. 8 Quote Link to comment Share on other sites More sharing options...
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