I had about a hour on dyno on Monday, was a bit of a fail really.
Everything was mint except for a consistant miss at 6500 rpm so I pulled plugs out to check gap and 3 broke! Fuck only found peasant hot as fuck plugs so couldn't really keep tuning it. Problem was a corroded contact in the dizzy cap for main coil lead!
Any way power it MILES up on old cam!
On 11 psi power was 225 hp atw when miss happened and didn't look like falling over anytime soon.
Torque is flat line all the way, will need to start tuning at like 2000 instead if 3000 as torque is already up there.
I really think 240 kw atw is possible next tune if turbo can keep up.