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GuyWithAviator's 1974 Austin 1300


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Finished the build and install of my original engine on Sunday. Took it for a decent drive today and it was perfect, just like a new car.  :-D

 

Few pictures of the saga: 

 

This was stuck in one of the water galleries of my og engine! Surprised it stayed as cool as it did

 

14324286911_9c35f0e476_b.jpgIMG_1668 by GuyWithAviators, on Flickr

 

And this is the sump plug of the smokey engine I'd been using for the past few months. Bits of 2nd gear I think

 

14325865052_8b90dcd50f_b.jpgIMG_2463 by GuyWithAviators, on Flickr

 

So the whole point of this rebuild was to fix this:

 


(Watch the whole thing)

Here's a timelapse of the final stages of the rebuild and install:

 

 

And to finish here's a photo of it during the drive today. Excuse the jacked up height, made it easier to work on/get jacks under

 

14327670635_8a521ec8b7_b.jpgUntitled_Panorama1 by GuyWithAviators, on Flickr

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Been dailying this everyday and it runs perfect. Doesn't get hot even at at 110km/h for a decent amount of time or just idling through traffic.

 

The WOF ran out a couple of weeks ago so went to get a new one - straight through no worries. Inspector told me that I should start thinking about sorting the sill rust out sometime soon.
I think Bornloser has some spares for me that K-trips sent down, must go get them at some point. 

 

Anyway yesterday as I pulled up the drive put my foot on the brake it went to the floor followed by the sound of liquid squirting out. Luckily the handbrake works well (on wet cul-de-sacs too  :-D )
The Repco brake light pressure sender that I bought 6 months ago for the last WOF had burst! 

 

14797874564_bfb7c16457_h.jpgIMG_9152 by GuyWithAviators, on Flickr

 

Went there today and got my money back but not impressed, a warning to those buying from Repco.. If that had happened at speed it wouldn't have been good. 

 

14820077723_fd2b24310f_h.jpgIMG_9154 by GuyWithAviators, on Flickr

 

All fixed now though. Nice new British made one from Butler Automart.

 

14797118621_d0ad77d919_h.jpgIMG_9165 by GuyWithAviators, on Flickr

 

Changed the oil and filter tonight since it was due after the engine rebuild. Old oil looked clean so that's good! 

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  • 5 weeks later...

If you're driving down Bealey Ave / Papanui Road in Christchurch today my apologies for the huge trail of oil...

 

14902158888_e57ddfa69c_b.jpg

 

post-11021-0-73967300-1409450153_thumb.jpg

 

The diff decided some parts were better off outside of it's casing. Not really sure what/why happened yet. It's strange though because it made a loud clunk (I assumed it was just Chch's roads) and continued driving fine but then I noticed the oil pressure light come on so stopped. 

 

Will have to take the motor out and split the block and gearbox. Luckily I have a spare gearbox but it's a pain :angry:

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Took the engine out and split the casings to see what had happened. 

 

14976579387_9d9b11f373_b.jpg

 

Familiar sight...

 

15160097601_33c7816c33_b.jpg

 

The spider gear pin in the diff had moved sideways because a retaining pin was missing and caught on something and snapped it in half, then the piece that broke off was flying around in there looking for a way to get out.  Surprised I didn't hear it.  Cracked the diff casing and the edge of the gearbox casing. Fell apart in my hand when I touched it.

 

15160093511_7c78cb1e4a_b.jpg

 

15140034536_5abfd226d2_b.jpg

 

 

15140045136_97279a8f5b_b.jpg

 

 

14976407180_ce0fb5ed02_b.jpg

 

 

The engine itself looks alright though, don't think any of the metal filings went further than the gearbox case.

 

Was hoping it would be a straight forward swap of my other gearbox but the gears inside don't look the best to will use the good parts from both to make a decent gearbox. 

 

15162698332_bdf4ec0aa9_b.jpg

 

But before all this happened the car has been running great and being used for daily duties. 

 

15140129596_b5e4e08b4e_b.jpg

 

Talk about it

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Decided that while it's off the road during the gearbox rebuild I'd make the inside a nicer place to be. When I first got the car I attempted to dye the original gross faded carpets blue again with some dye that you mix up in a salt water solution. Worse idea ever! It worked okay for a while then the carpet just fell apart even more and I noticed that the salt in it had made everything on the floor rust. 

 

This is the bottom of my amplifier

 

15089732730_2d2a6a3bc6_b.jpg

2014-09-13 20.52.09 by GuyWithAviators, on Flickr

 

And the seat mounts. Cleaned and painted all these up including the bottom of the seats and the seatbelt components.

 

15253433026_5f8b3d4621_b.jpg

2014-09-13 18.14.19 by GuyWithAviators, on Flickr

 

Because the carpet fell apart it meant that my feet were just on the metal floor which I did paint right at the start but it came off and combined with the water from the leaky door seals it started to rust the floor pan again. So I stripped that back and painted it again with several layers of decent paint this time. 

I bought a bunch of carpet from Bunnings ($25 per m of 2m wide) 

 

15276429685_9a8fd00b37_b.jpg

2014-09-14 17.37.22 by GuyWithAviators, on Flickr

 

(Can just see the corner of the OG carpet there)

 

Found all the sound deadening and then cut the carpet up to fit nicely! Was a bit difficult sorting the corners out but it looks really good for about $60 of materials compared to $280 for some precut stuff for this car. 

 

15253432846_b079565cc8_b.jpg

2014-09-14 16.33.43 by GuyWithAviators, on Flickr

 

The finished result: 

 

15089878317_1dbab965f6_b.jpg

IMG_2575 by GuyWithAviators, on Flickr

 

15276052592_48f0ca30e8_b.jpg

IMG_2577 by GuyWithAviators, on Flickr

 

Let me know what you think! 

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  • 1 month later...

Bit behind on updates, oops. 

 

The gearbox is all fixed now thanks to these:

 

15770234975_dc6d0c1766_b.jpg

IMG_20140927_195432 by GuyWithAviators, on Flickr

 

First test drive was to the McLeans Island swapmeet

 

15501746435_a96154ac50_b.jpg

IMG_6829-Edit-35 by GuyWithAviators, on Flickr

 

Went really good. 

 

Next thing that went wrong was the exhaust came off after the headers

 

15768402181_18acdcc89b_b.jpg

IMG_0366 by GuyWithAviators, on Flickr

 

Drove it around like that for a bit until I had the time to take it get fixed

 

 

Had a flexi joint put in yesterday

 

15585090777_d0e0662585_b.jpg

2014-11-11 11.06.10 by GuyWithAviators, on Flickr

 

And took it for my full license test today, the instructor loved it.

 

That's it for now, just continuing to get it ready for the long trip to Auckland in January next year 

 

15325553160_f31fd4df5f_b.jpg

Austin 1300 2 by GuyWithAviators, on Flickr

And a nice picture to go with it all

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