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yoeddynz

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Everything posted by yoeddynz

  1. I think if I spend any real money and effort at improving the fueling it'll be via a megasquirt/speeduino ecu and my own custom injection After having pissed about trying to tune an SU on my turbo rotary, the cost of needles and it never being right compared to tapping on a keyboard (or even my phone!) injection just makes so much sense. But for now I'm happy to just get a the stock hitachi system working. Certainly going to make a cold air feed though. Bart was right- its thermonuclear hot up in the top of the engine bay.
  2. Once again old man Datsun has stepped in with handy bits of knowledge I'll rule that torn boot out. The history and origin of this carb is a bit murky. I was given it by a Viva loving friend in Nelson who had got it with a box load of Viva bits. This was well before I had even contemplated buying an Imp, let alone a Datto powered one. So it sat in my big box of junk under the bench next to old dizzys, starters, alts etc with the idea I might retro fit it to the Viva 1159cc engine (apparently they work real well on Vivas) Hannah was the one who looked up the serial/model numbers and deduced its from a 1200. However- I have not confirmed that the jets are correct. So at some point today I'll strip it down and check the jet numbers, give it a proper good look over and see if I can spot anything. I dont want to wait for an ebay carb kit, nor wait for a potentially substandard carb from Ali. @Slacker_Sam. can sort me a carb kit for $50 which seems ok but we are yet to confirm whether it has new jets or not. No point me buying a kit without jets and then discover the jets are incorrect in this carb. I do like SUs but they never have the same snap in acceleration. They are great for economy but apparently, well from all the road tests I have read, these Hitachis are aweome for economy on a 1200 as well as having the extra acelleration pump feeling. Apparently. Its gonna be something stupid and small this issue. Anyway- we have a tiny house build to take on now and earn monies!
  3. What if the piston is buggered too? But yeah OK. I'll check it all out and see if I can spot something else. Meanwhile.. You be a good boy and look through your carb collection for me
  4. Why hey- thank you! You are most welcome here- should I put the kettle on love?
  5. Well I fixed one leak and then discovered the mother of all leaks.. Mr Bart- tell me more about your box of bits. I think its just the bore on base that is worn- hoping the shaft is OK. Although I do think my cunning use of a rubber washer and a blob of silicone has truely fixed that, now minor, leak and in a good Barry fashion I'm just sooooo stoked its road legal now.
  6. The little IMP is now all road legal !!!! I refitted the carb this morning, hoping for the best but it was still terrible. I just couldnt get it to idle below about 1500 rpm and it had a big flat spot on light acceleration. So I gave up and we drove it to town, the long way through Kaiteriteri so I could have some fun on the windy road there. Wow its fun! Soooo much fun. Even with an engine that wouldnt pull properly, horrible flat spots, tyres that are definitely too high in pressure, a few clanks from the yet to be fully secured pipework, noise from the un-insulated engine bay shelf, noise from no carpets, fumes being drawn in through the old heater hose routing holes etc etc... it was still fun. It really is like a big go cart. The steering is lovely. Gear shift is great. Brakes getting better as they bed in. The temp gauge sat pretty much bang on an indicated 80 degrees C whch I reckon is more about 90. Fan only came on when we stopped, as expected so I was really happy about that. We got to town and straight into the booked WOF slot. Our local friendly wof man just loved it. Kept saying how cute it was, how neat the install was etc. Really impressed. Did all the check things as usual, test drive and it was all good. We looked about all the neat stuff in his workshop.... WOF attained and we went to the local council and got a years license. $47 - yay for old cars. Did a shop at supermarket, did the proper look back over my shoulder at my little Imp, sitting there in a sea of bland grey modern cars, looking sooooo tiny. On the way home we popped in to show it to another couple of fellas who run a nice country workshop and had sorted out the tyres for me. They too loved it and the older fella reckoned it was running way too lean and certainly had a big air leak somewhere. Then off home, this time driving over the much steeper longer climb. No worries even with terrible carb. No increase in temp. Yay for that. I got home and removed the carb. Discovered two things. Firstly. Spot the schoolboy error here... Yep- That accelerator pump can go downwards for sure, but not if the lever pushing it down cant go up at the other end! My air filter base was stopping it. This also meant that along with only a tiny bit of travel I was also not getting the secondaries to open properly. Easily sorted with a hole, some alloy and some epoxy. Second thing- this... There goes my air leak. Air getting pulled in through that huge split, past the accelerator pump piston and into the venturi. Well at least I am pretty damn sure that this is the culprit! Reporting back with findings soon.....
  7. Hannah got to drive it yesteryear evening. She loves it I knew she would. Hannah's first classic was a little imp super she bought in the UK and she joined the imp club back then. Did a few local meets in Oxford. This was her first drive of one since then. We popped down to the beach last night... The little car is going well but for a stumbling idle. I cant quite tune it out because the throttle spindle was so worn. So last night I took the carb off and stripped off the linkages... The gap is quite large! .... I'll keep a look out for a better carb body but for now I have to improve this one. So I went through my collection of rubber washers and found one to suit, which I did. Its a good snug fit over the shaft and sandwiches in neatly between the body and the first bit of linkage... Then the other end. Nothing to sit a washer on. So I dabbed a bit of automotive silicone on top and let it set. It flexes enough to let the shaft turn so its now well sealed... I have yet to try it out. The car is booked in for a WOF today so wish me luck
  8. yeah for sure those pipes were only just touching..but it was easy enough to squash them so every little helps I'm over carbs already... looking forward to injecting it. But for now I shall persevere...
  9. Cheers. Yeah it sounds meaner then 68bhp (gross...) should do. That little carb is certainly holding it back. At about 4500 it starts tailing off. I think also that the E15 electronic dizzy might not have the right advance, nor does the vacuum unit I've retrofitted from some ford. Basically I'm going to get a replacement main chip that's missing from the MS1 that I was given ages ago and at the very least run full lecky ignition. Injection won't be far away.. But for now.. Drive it.
  10. Hey thanks - glad you enjoyed the read Yeah it was more to do with making sure the cooling system works well. And it seems to so far but yet to take it up a good hill....
  11. Righto. Exciting news. However I shall start where I left off. So last time I moved the car under its own steam resulted in quite literally its own steam, all over the floor when the heater matrix decided to give up. I swapped that out with a spare unit I had, replaced that seal in the clutch slave cylinder, fixed another couple of wee things and prepared it for the big drive. I also lowered the platforms on the front dampers and got the car down to a much better height. I may well raise the front by around 5mm later on so to get the camber a little less negative. I'm not a huge fan of excessive negative camber nor does it aid in handling unless corning at 9/10ths all the time. The car looks so much better low all round. I took some photos.. Now lets take it for a drive! This time I made it about 1 metre further then last time. Then I stopped to look for the cause of a terrible rattle coming from the flywheel/clutch area upon engaging the clutch only. I suspected the spigot bearing (which foolishly ...when will I learn... I thought was a bit worn but it would be OK..) Upon Hannah sitting in the car depressing the clutch for me to investigate the sound, the drive to the box stopped. Bug-ger! I thought it might be a broken friction disc hub etc. Same scenario as last time... push the car back in feeling quite a bit pissed off and this time we both went for a decent run. Get away from that car I thought! Proper exercise is my go to thing for instantly feeling happier So that night whilst in the middle of engine and box removal I discovered that the clutch slave had pumped out, again, and was holding the clutch in I released the bleed nipple and the clutch fork returned home So I now suspected two things here: Either the flexi hose had broken down inside and was restricting fluid returning quick enough so instead the master refills from the reservoir. So I had a new hose made to rule that out. Or was it the little one way valve within the master, of which I had made a new spring for to replace the missing item, opening too easily. Possibly it was easier for the master to draw fluid in quicker via that valve then refill from the returning fluid from the slave. Hence the slave was getting pumped out with each push of the pedal. It stayed out in increasing amounts by about 4mm each stroke! So I bought a new 'proper' spring whilst I was at the brake shop too. So there it sat- engine not exactly where it should be. But I do like this shot though... So out with the engine and trans. I made a wooden cradle this time which I lowered the engine into. It made it much easier and meant I was able to have the engine and box sitting on the large mobile steel bench and I could then work on it at a decent height. I removed the transaxle, then the clutch, adaptor plate and finally the flywheel. Gave all those bits a clean. The flywheel has been lightened quite extensively and weighs up at 6kgs. A standard item is about 9kg... Here is a good shot of the alloy adaptor plate that joins the box to the engine. Its quite nicely made... The spigot bearing was indeed pretty worn once I had a good look at it... It was indeed allowing the first motion shaft to just tap inside the release bearing guide tube. I bought some Phosphor bronze and made a new spigot bearing. No photo of resulting new bearing- but rest assured it looks pretty much like the old one but this time without enough room between its bore and the shaft to house several Badgers. I reassembled that lot and had a looksie at the transaxle reverse gear plunger... I was not happy with how much effort there was involved in moving the gearstick into the reverse plane. I knew what was 'grabbing' and had an idea on how to improve it... There is this lockout plate that rotates in an arc as you move the lever across the gate in neutral. There is a spring loaded plunger that has to be pushed in to select reverse. However the edge on the plate is very sharp and rather then sliding over the plunger as it pushes it in it digs in a bit. I could feel it through the lever. You can see it here... You can see scrape marks on the cone of the plunger... So I gave the edge of the plate a gentle tickle with the grinder.. I also took the corners off on the plate here... where they slide through the slots as you move across through neutral here ... Resulting in a much nicer shift. It will be improved further when I get a proper ball for my shifter and I suspect my flexible coupling at the end of the shifter tube onto the transaxle is a bit too flexy. The trans was reunited with the engine and slung back into the Imp. It all went back in nicely. This morning we re-bled the clutch system and YAY !!! It works better with the slave returning instantly. Filled the cooling system back up, having added a bled nipple on the thermostat housing which improved the bleeding of air from the system hugely. I'd also forgotten to mention that a fair while ago a fella on the Imp forum mentioned that my stainless tubes tat run under the floor should not really be touching each other all the way down. The hot one will heat up the cool one. Not good. I didnt think too much of it but it bugged me so quite some time back I ended up ovalising them which gave them clearance all the way down... I also made a throttle stop so not to break the cable... With that it was about time to go for a drive.. Success! This time no rattles from the clutch area, clutch worked fine, battery was good. Ran it up to temp and bled all the air out. Temp went up to about 80 degrees C indicated and sat there. It was a fantastic sunny and pretty hot Autumn day for a drive. All the smoke from oil spills, coolant spills etc burnt off. I checked the timing which was about spot on at factory setting. Gave the carb a tweak so the car idled nicer but it'll need more attention. It has quite a worn primary throttle spindle and I think that combined with that light flywheel makes it hard to get a super smooth idle. Enough is enough though. I finally took the plunge and did this....... I came back beaming. It drives pretty well. Wanted to stall when stopping, because of that lumpy idle. Has a slight flat spot down low but once on the secondaries it fair flies along (well.. for a Datsun powered Imp) It sounds much better then I was expecting. I parked it up and checked all the usual things. No obvious leaks and the fan came on after I adjusted the knob on the thermoswitch. Fan is loud but works really well- very efficient. Happy, relieved, excited. We both sat down on the sofa, had lunch and a cold beer and admired the little blue car in the sun. Yay
  12. I can swap for a weber 28/36 carb that someone gave me. Oh hang on.. That was you.
  13. No holes are getting put in the side, or anywhere visible. Its a sleeper. I don't want to give the game away that it has 68 ponies (gross..) waiting to be unleashed.
  14. I know... But baby steps first. It did have these on it when I first went to view....
  15. I'm a member of the datsun FB group so yeah - I can try. But actually it'll be more fun and satisfying to make my own and then it can suit the spot perfectly. I have a feeling that the Datsun item will still be too tall. Must do sidedrafts.....
  16. Yeah totally correct. I'd even been into Nelson looking for alloy ducting but the place that stocks it didn't have the size I wanted. I'd bought a pod filter for the job but it was huge and ugly. I was going to mount it down low. I realise it's gonna be fucking hot up there so yeah.. I need to do something. However I just wanna drive the thing and check every thing out so a top mount filter will suffice for now. Ideally I'd be sticking side mounts in place given the huge amount of room I have there but again.. I just wanna drive it. Imps generate a big vacuum area and the engines get filthy quick (shame) . Certainly have to have a good filter system. The southern hemisphere cars actually ended up with a feed tube from the drivers door frame due to our dusty roads. But it's too tiny for a bigger engine so I removed it and welded over the hole. Id spotted the c20 top hat thing on datto wiki. Looks ideal. Easy to find?
  17. Exciting times here at the only Imp workshop in the valley. It runs! But typically there are a few small hiccups. Some actually quite comical. I think we should re-wind back to where we left off last time. So I needed a new ball to see the gear stick through until I can get a decent proper replacement. I had bought a section of nylon/teflon bar. I made a gauge from card to match the curve inside the socket that the ball would rotate. Then I reversed that into a gauge that I could place over the bar as I machined it. Not exactly brain surgery. Which leads me to a little giggle about this bit of comedy gold... https://www.youtube.com/watch?v=THNPmhBl-8I he he. Love it. So yeah.. easy job. I got a pretty match and it came out OK. Works well enough but the reverse lockout plunger spring is a bit too keen and popping the gearstick left into the reverse plane requires quite a sharp movement. Luckily it would be easy enough to sort, except for that removing the engine and box bit.... I might just put up with it. At least I'll never accidentally select reverse when dropping down into second before hurtling around a tight corner feeling the full force of the mighty 68 little Datsun Ponies as they rocket me forwards. But before I got too excited about such F1 levels of performance I thought it might be prudent to protect those little Ponies from breathing in dusty air. I needed an air filter that fitted the space I had (not much area in height available), looked good and was cheap. There was nothing available. So I'll make one. I started with an old but perfectly usable filter from a customers Ford econovan (Mazda really..)... I chopped it up, essentially slicing off a section of the right thickness to suit the height I had. I then grabbed a section of 5mm alloy sheet I had in stock, chopped out two discs with the Jigsaw. Put a hole in one with a holesaw which allowed me to hold it in the lathe to machine it down. Reduced the thickness by 3mm leaving a neat lip around the edge to not only hold the metal filter outer in place but hide and seal the edges... For the lid I welded an old steering wheel boss I had kicking about onto the plate. Then I machined the plate down to suit, like the bottom one and then cut the boss off. Cleaned up the marks and ended up with a filter that fits and looks the part too. I'm very happy with it In place... Note the ugly pipe hanging from the rocker cover breather. I need to sort out something there. The manifold the carb sits on seems to be spot on level since modifying it. Welding castings like this can often be a bit tricky what with porosity and dirty alloy. The datsun item seemed quite clean in this respect... The tiny little Hitachi twin choke carb that sits on top is so dinky. I have no idea exactly what model A series engine its from as I had been given it by a friend who had got it with a job lot of Viva parts. I can only hope that the jetting is correct. I'll soon find out. I might try again with research on the numbers. I had to reconfigure the throttle cable layout to suit its new home. This involved a new pulley to suit the cable pull on offer from the stock Imp throttle pedal... So the filter was sorted, carb in place, cables all hooked up (after buying 3 metres of Shimanos finest brake cable outer to suit the stainles brake inner for a tandem bicycle) and it was all getting a bit exciting. I was starting to get those 'first start, will it start, will it blow up, is the engine actually rooted?' feelings and thoughts. I double checked everything and put some petrol in the tank. No coolant yet- no point if the engine turned out to be a plonker. It would only be one more thing to have to remove. Turned the key as Hannah excitedly watched the engine from the back... Whir, whir, whir, whiiiir, whiiiior, whiiiiiooooouur, whiiiour, whour, wooohour, woooooouur, woor, woor, woo, wo, w....w.. Bugger. Well that battery that charged up ok, seemed ok, was obviously not OK. So we connected the booster pack on. Winding winding winding. Nothing. Hmmm. Has to be spark. Fuel pump, barnd new, was working fine, fuel at carb and at correct level. Fuel smells from exhaust. Spark then. I checked the coil- yep. Power to the coil. I checked it had power when turning over (some ignition switches can fail like this). Yep all good. Checked for spark with spare plug on lead. Nothing. Checked on king lead. Nothing. took cap off and checked rotor. Good. Checked continuity on leads to and from coil to electronic pickup in dizzy. Fine. At this point I was getting a sinking feeling that the pickup module in the dizzy was broke. However I knew that the previous owner had the car running not long before I bought it and there was nothing I'd done that could break it. I checked the polarity on the two wires. It was correct according to the electronic ignition swap thread on Datsun 1200 wiki. i had a look at all the photos I had taken of the wiring before I pulled the car apart. Hmmmmm- the two wires are the other way round. I did some more quick googling and it seems that they should be that way. Tech wiki- you lie. Swapped the two wires and this time we had spark- which my hand can attest to as it had 20,000 volts jolt through it. Reconnected plug lead, tried again and this time something. A muffled backfire. Tried again- same thing. Hmmm- timing is way out. Dizzy timing and it was fine- I had previously very carefully setup TDC using the stick and two marks meathod to double check the marks on the crank pulley because the car has got Toyota 5 rib pulleys on it (previous owner had at one point been running a supercharger on this engine) Everything seemed fine. Then Hannah quipped up and said "maybe its 180 degrees out and its on the exhaust stroke?" She was correct. I had spent all that time checking the tdc but not properly checked if both valves were closed. Oh silly me! So we spun the dizzy round and reset its timing. Jumped in the car and on about the second go it started. Yay!!! It sounded good. Not too noisy. Ran it for half a minute, workshop filling with smoke as all the paints, spilt oils, greasy finger prints burnt off. Decided it was worthy of some coolant and so Hannah filled up the system. It took ages to swallow about 9 litres of coolant, even with the bleed nipples open up front. sadly there was a pinhole on the thermostat housing I'd repaired and the old Smiths temp gauge decided that because its parent company was Lucas it would wasn't going to turn up to work. It was getting late so we called it quits and I removed the housing to seal the pin hole. I swapped the gauge over for another one and went to bed. The next day I thought would be the day of the first drive. I excitedly put the number plates on. I didnt want to fit the rear plate in the usual position on the engine cover. There are no holes there, no light, no light mount and the plate is too wide that it akwardly covers over a section each side of the main centre hole. So I drilled two tiny holes and mounted it below the bumper, with a light on one side. I think that I'm going to change the light though for a neat one hidden in the un used and slightly bent crank handle hole on the bumper. But back to the that drive. ooooooh exciting. So exciting I had to go have a nervous poo. Once back I started the car, with the help of the jumper pack and warmed it up a little. Clutch in. oh. That feels weird?.. let the clutch out eased the car out of the workshp into the sunshine, first time this shell has moved under its own steam for a very very long time. Awesome! Righto- lets go. Then suddenly.. gurgle gurgle splatter splatter. Coolant starts running out of the heater onto the passenger floor. Bugger!!!!! Arrrgggggggghhhhhhh! Righto- thats it. I'm over it. We pushed it back in to the workshop, into the corner of shame. I muttered some more choice words and then said to hannah "fark this...Lets go for a bike ride" So we jumped on our cyclocross bikes and went for a strop in the local mountain bike park. I got to contemplate the problems and felt much better once we got home. Then this happened... I had the heater matrix out and on the bench in about one hour of the Craig Charles funk and soul show. Turns out it had frost damage, from cold Canterbury days sitting out in winter (this heater was from Imp 3, the Christchurch car). Luckily I had a good spare!... Then that clutch. It had over extended itself and when I tried it again once back home it pissed fluid everywhere, having jammed a seal... I have swapped in a spare seal, extended the pushrod so it starts from the very start of the piston travel and will watch it- you can pump it out with quick clutch foot action so something aint right. I suspect its the flexible line has inside kink. I'll look to replace it. In normal use the clutch seems ok. Time will tell. Well that was a wall of text! I hope you all enjoyed my ramblings. Oh and the spare temp gauge I fitted is crap too. I'll buy a new complete setup. I promise the next installment will be full of joyous Imp driving tales
  18. Wow. As the new title suggests. All those little jobs. As all those who have or are undertaking a car project will agree these little jobs certainly do add up. I can skip them or rush them especially as the canvas upon which they attach is so clean and tidy. So is no particular order, due to the fact that some of them I start, then stop when I realise I am missing a vital part which has to wait until the next visit to the big smoke, start on another job in the meantime, go back to last job, forget where I was at with it, then realise I forgot to get the bit even though it was on a list, then start on another bit. While all this happened there was also a fair bit of mini adventures going on because Hannah's brother was over from the UK on holiday. We did some very nice camping, biking, hiking trips with him. Because we all like pretty pictures here's some from a few of the adventures had in a last few weeks... So yeah- working on a car project is tricky when tempted by the outdoors like that Back to the Imp. First big job since the last update was to sort out the wiring. I basically re-wired the whole car. The original layout was not going to work how I wanted it to. There was a fair bit to add for safety, extra features, ease of disassembly, neatness. I bought an extra fuse box as I realised 6 fuses were not enough for what I wanted to do. Photos.. The wiring shop.... I have a fair bit of automotive cable I have collected over the years to use... I mounted the boxes and relays onto a piece of clear lexan. It worked out a very neat way to do it. I also took the instrument cluster apart and cleaned it out 50 years of dust. You can see the amount of connectors that have to be undone to remove the instruments... It just does my head in when I am so used to a couple of plugs, even on the Viva which is the same era. So I added multi pin plugs to the loom. Easy now. Fuses and relays in position... The race car came with an extra gauge pod below the dash. I bought a new electric oil pressure gauge, got given a very neat wee rev counter by my good friend Dean (cheers!!! ) and kept the Smiths temp gauge in place. I didnt like the way the pod was wider then the heater control bracket I was mounting it to. So I made a tapered mount to fit between them.... Gauges and dash etc as it now... Other things added were a neat wee push button switch for an electric washer pump because all the squeezypush type squirty rubber butons had perished. I added extra wires for a stereo, amp, electric water pump, under dash footwell lighting etc. Moving to the back. I re-wired the whole lot. Not much to see because all the wires are now tucked out of the way. I needed an alternator belt tensioning bracket. The datsun item was horrid.. So I made a new one. However I cocked up and soon found out it didnt quite line up. I had to had a bit.... In the end it turned out sweet and I'm very chuffed with it ... Now moving up to the front. The battery. It needed a home so it wouldn't slide about. I made an alloy box from some thin sheet. It bolts in place to some alloys bars attached to the bulkhead so i only need to remove two cap screws and it can be removed if I need to take the tank out etc. In photos... I made a stainless bracket to take a washer bottle, of which I can not remember where I picked up but have had for years waiting to use on a project. Finally a home for it ... Heater tap. I needed one. The Imp one was knackered so I went to the wreckers and got a couple that would work. Picked the best fitting. I think its from a Honda. Really neat item and should last. Would be an idea replacement for a stock Imp setup too. However I am running both hoses, inlet and outlet, from one side now where they tee off from the main lines. Anyway. Photos. I needed to adapt the old brass fitting so I machined it out and soldered in the straight section of the old u angle pipe... Altered the Honda bracket and made it all fit... Played with some hoses... and ended up with this... Clutch time. hannah and I had a hell of a time trying to get it to bleed up. I finally worked out two things. Firstly- the replacement seal that I had been sold by a 'reputable' brake specialist was the wrong one and its heel diameter was slightly too large meaning the piston was struggling to return. It was a friday, no chance get another so I went through all my seal collection and found this... However it was too large and wouldn't fit. I looked again. Next up out of the box was this... Still no good! Bugger. So instead I machined a new piston to suit a seat that was the right OD but had a larger ID... Now the piston returned. But it still would not drag in fresh fluid. I took the master apart for the 14th time and looked at some other diagrams online. I soon realised that there was a teeny tiny spring washer missing behind the rubber inlet washer. Its not visible in the Haynes manual or mentioned that I could see. I made one from a coil of spring and now had a fully working master cylinder. The clutch bleed up pronto and works fine now! Phew. Latest job I did was last night. I removed the exhaust and added a boss I machined from a 18mm nut for an O2 sensor. Then I was mucking about prepping an 18mm bolt to make a plug for the time being and remembered I still had not only a boss but also a stainless plug left over from the Innovate wideband kit I had fitted in the V6 Viva. Sweet. A nice treat. And that is all for now. Its getting very close. Engine has a new oil filter and oil, coolant needs to be added (and I bet some leaks will need fixing....) and then I just need to make an air filter assembly for the carb. Nothing available to fit the space, at a price I like, so I will build my own from one 5th of a Mazda Van filter I also need to machine up some Nylon bar I bought to make a new pivot ball for the gearlever. Big thanks to John875 from Australia who bothered measure one of his balls for me and post a photo online. It looks like this...
  19. Ok cool. Could be a source for new cheap jaws. Most I've seen are all the same size.. All copies.
  20. Your shrinker stretcher. What make is it. Do you find that sometimes the shrinker jaws won't 'grab' the steel enough to shrink. I've cleaned the little ridges on my set of shrinker jaws but I think they might be worn. Sometimes it takes several attempts to get them to grab the steel.
  21. Yeah - they have moved back further now. Trailing arm suspension.
  22. Thanks dave. Just did a, hopefully last, shipping mission for parts in Nelson. All those little bits adding up. Running out of moths. Bought a pod filter from supercheap. Extra 15% bhp right there. I have been gifted 3 days to myself to work on imp whilst hannah is off tramping up in the Mt Arthur region with her brother.
  23. Fuck this is looking so good. So close! Please-never ever paint it.
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