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Andy's 1974 escort GT


andyball1

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Hey guys

newish to the forum so thought it'd be about time I sort out a build thread for my new pride and joy!

Disscussion thread- //oldschool.co.nz/index.php?/topic/35479-andys-1974-escort-gt-discussion-thread/

Last year my best mate bought this onyx green mk1 GT in the idea to restore her and give it to his mrs for a present.

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The plan was panel, paint, wheels and a 1600 motor. Sadly after afew weeks he hated the car because he should of bought a 2 door and lost interest.... so i bought it :) happy as a pig in shit!!!

so we proceeded with the plans of the rebuild.

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as the car still had the original paint is was pretty clear where the problems were, but unlike other mk1's this thing was near rust free except the small squares in the rear wheel archs!!

once the rust and panel beating was taken care of we went through and started the painting. the colour is a hard one to photograph as it seems to come up white on a camera but it is actually a very light blue.

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now with the car all painted and looking spiff we started by bolting in the newly aquired 1600 mk2 motor

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once that was done time to put it back together to ship it to my workshop to finish

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but before trailering it away i had to play with the new shiney toys that turned up

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And they see me rollin....

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now latest work is ive started bolting it together started at the back as i was feeling lazy! my goal is to have it running for xmas.......

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now on the rear end you see its black like some Gt's were now does anyone have the chrome trim for around the arse end of the car?? im struggling to find any!

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  • 5 weeks later...

well small update time

didnt get the car done for xmas but am getting closer ive now only got afew things left like windows, exhuast and finishing off the wireing in the engine bay. have booked a full day off work so i cannot get bugged by the wife and get some work done for a change!

have just bought myself a set of coby extractors that will go with the new system thats being made as soon as its running.

also ordered some new toys from the uk like a short shifter, quater bumpers and a full nut and bolt kit so ive got nice new shiney spares!

another update and hopefully on the 11th :)

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  • 2 weeks later...

update time

worked on the car this weekend and got the engine bay all wired up no worries, BUT as always was just testing that the starter motor is wired up right the motor turned over once and then seized tight! FFS!!!

So we ripped out the motor that was supposed to be a mint runner, then as i removed the gearbox i find a pink rag wrapped around the whole shaft, clutch and flywheel jamming it solid. FFS!!!!

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See the rag in pink above

well motors fine so put it back in and wired it all up and tested it and it now turns over loverly

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now all i have to do is finish the custom throttle linkage, fill it with oil and water and hook the clutch up and thats the engine bay done!

BUT ive got one small problem. i cannot find the wires for the windscreen washers in the engine bay? anyone know where i will find them??

could this be the wires for the switch inside??

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any advice would be great!!

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  • 2 weeks later...

hey guys

small update that will follow with pics soon.

ive now got the motor running mint and the glass all in. all ive got left to do it the drivers seat bolts, bleed the brakes then its off to hamilton for a exhaust and a wof!!

car is currently getting a rush prep for the Cannonball run thats taking place in aucks next weekend so once it survives the run itll go back in the shed for the tidy up etc but for now ill be happy to just have it running on the road.

car is looking good! will post pics monday once i get my A into G :)

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well from above motor was in and running mint. seats were in and car was complete so i took it into hamilton to get exhaust done and a wof check

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after a fight with a new master cyclinder being made wrong and a few touch ups she got her wof no probs! Huge thanks to the guys at The Muffler shop for makinf a awesome sounding exhaust for my car and helping finish her!

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BUT................

day of cannonball run and the car was stickered up ready to go

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we heading up to aucks at 6am and noticed the car was really low on power for a 1600 which we thought was a tad odd but we carried on and made it to the start line.

after 3 odd hours of driving and we had just started hitting the first hill of the coromandel and poof! running on 2 cylinders banging and popping away :( pull over to find oil everywhere!

we clean up the engine bay and find the crankcase is preasuring up and blowing the oil out the filler neck and dipstick hole! but only when the motors under heavy load??

so we turn round, roll down the hill and make the slow crawl home :(

so sadly its either rebuild or shop for a new motor by the looks. from what i can guess my rings are rooted as the filler neck is chuffing BIG time :(

oh well she looked good i reckon!

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