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Cam's Toyota AE86 Trueno Racecar


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I think I have a problem. Sitting in my shed is now another AE86 which brings the total to 3. The story goes something like this...

I've been building my other racecar for something stupid like 6 years now and it's still a reasonable way from being ready to make its first outing. This is for a whole bunch of different reasons, primarily lack of focus and laziness I guess. In some ways this doesn't really bother me as I find that at least half the pleasure of the car is being out on the gargae working on it. BUT at the end of the day I started building it to go racing and in the past 6 years all I've managed is a few trackdays in my Silvia. So, when this AE86 came up on trademe I decided that enough was enough and that it's time to go racing. At the very least this should provide a shitload of motivation for getting my other car finished as I'd much rather be in something that I've built myself rather than simply bought.

This is the car as it sits now. Photos are straight from Trademe as I'm slack at taking photos myself. Excuse the colour - I'm not sure if I can't stand it, or if it's growing on me yet.

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It's now sitting on different wheels that make it look a heap better than in these photos.

The basic specs are:
Excellent condition AE85 shell which was race prepped in 2004
Recent respray
Facelift bumpers and factory boot spoiler
Brand new Jamex race seat
New harness
Fully homologated cage (basic but tidy 6 point design)
Comprehensive set of gauges
Awesome monster tach with shift light :rolleyes:

Bigport 4AGE
Wiseco 11.8:1 forged pistons
Ferra oversized valves (Formula Atlantic spec)
Ported head (more of a tidy up and port matching really)
Adjustable cam gears
Reground factory cams (unknown specs but appear to have decent lift)
Fully balanced
ARP rod bolts
7.5L race sump
Twin Dellorto 45 DHLAs with velocity stacks
High volume oil pump
Alloy radiator
Oil cooler and remote mounted oil filter
Coby extractors (I think) with side exiting exhaust
Electric fan
Davies Craig electric water pump (no thermostat)
Facet fuel pump and Holley fuel pressure regulator
Link Storm G4 computer running ignition only
Full rewire (no indicators, headlights, etc)
Tuned by Bob Homewood - was apparently putting out 144 HP @ wheels

T50 gearbox with short shifter and obligatory TRD gearknob
Hi Lux LSD differential with 5.3 gears (also came with a 4.89:1 CW&P)
AJPS FC RX7 front brake conversion with Honda 265 mm front ventilated and slotted discs
Nissan Cefiro rear
Brand new Ferodo race pads all round
Billstein shocks all round
Adjustable height coilovers in the front (unknown springs but I suspect they're King springs)
King springs in the rear
Adjustable castor arms
Front and rear sway bars (both factory AFAIK)

Toyo R888s in 195 x 50 x 15 (6 meetings old)
15 x 7 alloys (Avantis apparently)

I'll go in to more detail in the next post.

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I've been building my other car to race in the relatively new All Classic Japanese Series which is run at Puke and Hampton Downs. The series is aimed at Japanese cars 20 years or older and is a lesser expensive way to go racing than say SS2000. The guy who started the series is Steve Melhuish and the series is basically designed around his (ex) car - the car that you see here. When his car came up for sale it made sense for me to buy it as it's a perfect way for me to get into the series I want to eventually race in with my other car - just a lot sooner.

I think he sold it because he got frustrated by never actually using the car as he's always too busy running events. He's certainly sunk a lot of cash in to it in his last 4 years of ownership and I think it also was starting to look like and bottomless money pit.

The car was not running when I first went to look at it but I was told that it was an ignition fault and the motor had a bad earth or something like that. Apparently it would pop and fart but wouldn't fire up. The next weekend I called Steve to see if I could go and have another look and take it for a drive. When Steve told me that he hadn't had it fixed yet I saw an opportunity to grab a bargain so I made him an offer for it as-is. He accepted the offer and we agreed that given it passed a compression test (to help confirm that it was an ignition fault) that it would be mine! The next day I went and compression tested it and cylinders 2 and 4 were both well down (65psi compared to 165psi) so the deal was off. Steve at this point was pretty pissed off (with the car) so I decided to call it quits and bail out. Later that day he called me back with deal that I couldn't refuse that included his single axle car trailer so it was all back on again.

Some history about the car:

It was built up North in Whangarei in 2004 as a Targa car. I'm pretty sure it never raced in any Targas but it was raced in a few hillclimbs and other club events. Steve bought the car 4 years ago and stripped all the road racing gear out of it (passengers seat, foot rest, etc). It looked like this when he bought it:

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I think the paint looked a lot better back then....

It was then raced in a few Auckland Car Club events and eventually Steve started the All Classic Japanese series after he was unable to enter the Arrow Wheels series due to the car not being of British of European origin. I think the car's only done about a dozen events all up since it was built!

This was what the car looked like in September of last year:

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So with the purchase of another car it became apparent that the double garage here at home wasn't going to be enough so I managed to find a empty double garage about 200m from where I work. It's 36sqm, has power and water, and is locked up behind a really solid set of gates. This gives me somewhere to not only store the cars but also somewhere to store the trailer as our driveway is already overflowing.

I actually got the car started and drove it the few hundred metres from work to my shed. It was running rough as guts - not at all like an ignition fault. When I got it into the shed I did another compression test, this time on a warm engine and with the throttles open. The issue immediately became a lot clearer. I could hear the air getting forced back out of the inlet port on the compression stroke on cylinders 2 and 4. The motor definitely was suffering from a lack of valve sealage so the head was going to have to come off.

I started to strip the motor and Ned and another mate, James, gave me a hand to finish it off on Sunday. It's such a pleasure to work on after having been stuck under Neds Alfa 155 for the past couple of weekends!

Excuse the camera phone pics. Courtesy of Ned :)

Rocker covers off, getting ready to pull the cams out

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Cracking the cam caps

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Head off - bores look ok for a race motor. Honing marks are still there, with some scouring. Will check for broken rings and only pull it apart if I need to.

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Table of bits

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Combustion chambers - looks like its had a hard life but everything still where it should be. No signs of bent valves or interference. No signs of detonation or of a blown head gasket. Running rich but not excessively. Pretty positive really.

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Tucked in for the evening :)

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More about the diagnosis tomorrow...

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I have a shit load to write up but I'll try and keep the words to a minimum. I didn't have my camera for a few days so there's a shortage of pics to post up.

On Sunday night I pulled the worst looking valves out of the head. Both the inlet valves on cylinder 2 and the rearmost valve on cylinder 4. I could clearly see that these valves had not been sealing as there was carbon in the inlet ports. I was expecting to find pitted valve seats or burnt valves but they all looked fine. The main observation was that the sealing surfaces on the valves were visibly concave which looked like where my problems lay. Before I had pulled the head off I checked for valve clearance and all valves were fine so at this point I thought the damage was just due to a hard life.

So on Monday arfternoon afternoon I took the head to Tony at Lynch Built Engineering so he could have a look at it. He agreed that the valves I had pulled out were the worst of the bunch so we spun them up on the lathe to make sure they weren't bent. There was no evidence of any contact between the valves and pistons but this confirmed that the valves were all good. Next we put the worst valve in the valve grinder and it was immediately obvious what the issue was. Not only was the sealing surface very concave but it had worn out of round so only 1 side was sealing at all. With a decent grind it came back to life though so that was great news. Valve grinding machine:

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We resurfaced the valve seat with a tool like in the photo below, and that also came back to life. There was no evidence of metal discolouration so this was another piece of good news :)

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All of the wear is due to the motor being in the car since 2004 and with a hard life of high RPM it's taken its toll on the valves. I left the head with Tony so he could pull the rest of the valves out and tidy everything up. I'm going up on Sunday to lap the valves in and complete the remainder of the machning.

While I was there we noticed that there was a lot of green residue on the cabs from the race gas. It looks like the fuel has been overflowing out of the various ports on the carbs. Tony asked what kind of fuel pressure regulator I'm running and when I told him it's a Holley he said that this was likely to be the problem. Apparently there is a inherient fault with these and they don't regulate properly. The ball bearing does not seat correctly and they need to be modified. We're going to sort that out on Sunday too. I'll find out some more information about what the issue actually is for anyone who's interested.

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On Tuesday night I headed to the workshop to make a decision on wether I'll be pulling the bottom end apart or not. All of the bores are showing some signs of wear but only a couple of the marks are big enough to be felt with my fingers. My concern was that if I did pull the bottom end apart that I'd run out of money to get it back together before trackday. Rings and bearings aren't cheap for a race motor and who knows what else I might want/need to replace.

So I did a simple test to test the condition of the rings. I cleaned each piston and bore with a clean rag and turned the motor over until all the pistons were at the same height. I then poured 50mL of Kerosene into each bore. What we want to happen is for the level of each bore to drop at the same rate. If there are any broken or rooted rings then the kero will leak faster. My motor took about a hour and a half for cylinder 1-3 to drain out. Cylinder 4 was still going strong 4 hours later. This just means that the rings are a bit gunked up on this cylinder. I know a good way to fix that once I get it all back together though :D I'm pretty stoked that nothing seems to be beyond recovery. It looks like I should have this motor ready to go again for around $600!

So far I'm looking at:

Head machining $150

Gasket set $120

Cambelt $40

Tensioner $35

Head gaset $120 (assuming I can run a 0.8mm TRD one)

New oil $100-150 (need to change the oil once I've bedded it in)

I also pulled some of the wiring apart as it was looking a bit rough. I'm going to replace the connectors on the water pump and fan with DTM connectors like this:

DTM_pic.jpg

They're a really nice aerospace/motorsport connector that's fully waterproof and good for 7.5A.

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Here's a pic dump from yesterday. I'll come back and tidy this up later.

Aside from the bad motor there are a number of other things that I'm changing on the car while I have it apart. Well, that's my excuse, mainly it's because I'm a picky bastard... I also thought this car could do with a bit of Colin Chapmans 'add lightness' mantra added to it. The main change is to ditch the power steering setup that it had. I don't see any reason to have PS on a circuit car. It adds weight, adds rotational mass, reduces driver feedback and it's just more shit to break. So yesterday I pulled out a manual cross member that I had sandblasted a few months back and dropped it at the powdercoaters.

Before:

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I should have after photos on Tuesday :) I'll also recondition this spare manual rack that I have and treat it to some Urathane bushes from AJPS.

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The offending item:

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Here's a couple of better quality photos of how the car sits at the moment

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There's a whole bunch of other stuff I'm going to change too...

I hate this overflow bottle for some reason. Going to see if I can make a standard AE86 one look at home in the engine bay.

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This external oil filter needs to be flipped up the other way so it doesn't drain every time the car is turned off. The sooner the oil pressure comes up the better I reckon. It also makes oil changes far less messy. Can anyone think of a reason why this is a bad idea? The battery tray can also come out. I need to think of a tidy way to remove it without using the angle grinder and getting metal everywhere - I'm thinking a milling bit in the drill.

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The thermostat bypass (near the bottom of this pic) needs to be blocked off as there's no longer a thermostat in the car. At the moment it allows hot water to circulate directly back into the motor - not such a good thing :rolleyes: I also need to tidy up the heater pipes as they've just been looped (same as the heated throttle body pipes). I want to retain the water flow from the back of the head so I can stop air from collecting back there but I'll do what I can to tidy them up.

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I also want to swap the good set of bumpers I have onto the car as I hate the painted rear bar that it has currently and the front currently has a big hole cut in it for some unknown reason.

I pulled the crank pulley off so I can replace the cambelt because Ned spilt oil all over it :) I'll replace the tensioner while I'm at it. I have an ally pulley that I bought for my 20V motor a while back and I'm hoping that I can use it on this motor to drop some rotational mass. It has a 0.75mm offset that you can see in the photos. What's the maximum offset that I can get away with? I'm thinking that I'll machine up a spacer to slip on the crank before I put the pulley on or somthing.

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More to come soon!

Let me know what you think here

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I pulled the exhaust out so I could remove the original AE85 fuel lines that were still in the car. While it's out I'm going to wire wheel everything and paint it with some high temp paint. I also want to sand/machine the face that bolts to the motor because it had a heap of exhaust poo on it so I have a feeling that it may be warped. I really like the design - pretty much exactly what I'm doing on my other car.

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So then I ripped out the old fuel lines. Partly to save a few grams but they also just make an unnecessary mess of the engine bay. All the rubber mounts weigh a surprising amount. I've replaced them with P-clips to hold the brake line.

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The carbs got a birthday so they're now clean and ready to be reinstalled :)

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The sump makes me happy. Having to buy 7.5L of oil to fill it does not.

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Got the valve gear back into the head yesterday.

Pulled the old valve guide seals out.

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Success!

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All valves re-ground and ready to be lapped.

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Valve seats re-cut.

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Before.

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Add paste.

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Roundy round.

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Sorted!

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Cleaned the head. Fuck this took ages!

Before.

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After.

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Inlet port. Nothing fancy - just cleaned up. The ports are too big on these motors anyway.

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I put the new valve guides in, cleaned the valves and associated bits and put them back in. It was getting late in the day so no photos. Here's the head looking all shiny and new :)

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Now I just have to replace one valve guide seal that I messed up. Grrrrrr. And re-shim it. Should be doing skids this time next week if everything goes according to plan :D

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Just a quick update from the past couple of days.

I stripped the paint off the radiator support bar and dropped it in to be powdercoated. This photo is pretty shit but you can see the bonnet latch bar on the right that was on the car when I bought it. It's completely unnecessary as the car has bonnet pins, so I pulled it out. It bolted on to the radiator support panel so I also removed that part by grinding away the spot welds (the piece on the left). Underneath you can see the partially stripped, modified radiator support bar. I should get it back from powdercoating early next week.

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While I was at the powdercoaters I picked up my crossmember. It came up really well considering I had let it get a bit rusty. I need to pull finger and get the manual steering rack sorted ASAP.

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I gave the water lines for the heater the chop. As I talked about previously there is no heater core in the car but I'm going to retain the water flow from the back of the head so any air bubbles that bubble up from the block will not get stuck there and cause hot spots. I'm not changing the water flow, it's just to tidy the lines up and to get rid of the heated throttle body connections. I'm going to put a swage back into the end of the pipe and gold passivate it this weekend :)

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I started doing the little bit of rewiring that I talked about before. Instead of using DTM connectors I chose to use Weather Pack connectors. The DTMs are only good for 7.5A and this fan can draw up to 9A so I had to find something alternative. These connectors are good for 20A, are fully waterproof, and are available from Pan Pacific for pretty cheap. The fan originally had shitty spade terminals on which are complete crap for this application as they have no locking mechanism and obviously aren't waterproof. I cut them off, sheathed the wires in glue lined heatshrink and then installed the new connector.

Before

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After

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Probably could have had less photos for just a connector but motorsport electronics is my thing :)

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Lots of stuff has been happening over the past few days. I want to post photos in a more grouped fashion so I'll wait till a few things are fully complete before posting photos. The main things I've been working on are painting the exhaust system, fixing the wiring in the engine bay, calculating the compression ratio, polishing bits, drilling holes in stuff and building some electronics so I can control my water pump with the ECU. I'll post photos of all of these bits when I've finished them.

On Saturday I went back to Tony Lynchs place to finish putting the head back together (or so I planned). The first thing I did was install the replacement valve guide seal from my mishap last weekend and finish putting all the valve springs back in.

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This is when we realised that things were about to get messy as the cams have been reground to an unknown profile by the original engine builder. So I have no idea what the valve clearance should be or what the cam timing the engine needs. To sort this out I'm going to get the cams profiled by Franklin Cams in Pukekohe. For $35 I'll have a complete picture of what these cams have been ground too which is pretty sweet. I have a feeling that the cams are holding back some performance from this motor so this will also help me to figure that out too. The less unknowns the better...

But while I had everything there I figured I would measure the valve clearances and the current shim thicknesses so I could save some time later on. I put the cams back in and came up with this.

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The only issue is the fucking towel I had the head sitting on got picked up by a lot of the valves as I turned the cams so all my clearances are full of shit. Grrrr. At least I know the shim thicknesses now. I'm going to redo it this week.

So with the rest of my day I went about cleaning up all of the water fittings and re-plating some nuts and bolts. It's a lot of fun to see scungy old bolts become like new again :D

As I was talking about above I'm tidying up the old connection points for the heater core so I can retain water flow from the back of the head but not have a spiderweb of old water lines going everywhere. So I gave the pipe that goes on the back of the head the chop, re-swaged it and then bead blasted it.

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Then the pipe that runs rearward from the water pump got taken care of. Gas welded the hole where the heated throttle body line used to attach, swaged the end, tidied up the mounting face on the sanding disc, then zinc plated it with a gold passivate. I think it looks the tits!

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The bypass pipe that allows water to flow from the head back to the water pump when the thermostat is shut is now surplus to requirements as the car no longer has a thermostat. The easiest way to block up the fluid path was to plug weld the bypass pipe and put it back as normal. I tidied it up and re-plated that too. My gasket set only came with one o-ring so I need to find another before I can put it back together though.

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Next I took all the aluminium water fittings and sorted them out too. I resurfaced and sealing surfaces with the sanding wheel and then bead blasted them all. This sort of work is really fun as the difference is huge and it doesn't take long when you have the right tools. A big thanks to Tony for letting me use his workshop!

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Finally I took all the mounting hardware for the head and re-plated it all.

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So this week I will start putting all the water fittings back on the head and block. The cams are getting sent away tomorrow and it's a 1 day turnaround so by the end of the week I may even have the cams in and have it all shimmed up :)

Next post I'll write up about the zinc plating process....

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  • 3 weeks later...
  • 2 weeks later...

Ok it's been way too long since I've updated this thread. Got too busy before trackday...

So I wanted to do a bit've a write up on the zinc plating process because it's pretty sweet. Tony Lynch has a really nice little electroplating setup at his workshop that's perfect for doing nuts and bolts and other small items. The process you see here is exactly the same in a fully commercial setup, just on a smaller scale.

As you all know when you leave steel uncoated it corrodes like a bitch and soon you're part has turned into a pile of rust if it's not protected in some way. There's a heap of different ways to protect the metal like painting, powder coaring and galvanising. Galvanising is the process of coating a metal (generally steel) in zinc which is less prone to corrosion. The zinc acts as a sacrifical anode and protects the steel underneath. The zinc is normally applied via an electroplating process however it can also be applied by dipping the part in a bath of molten zinc (hot dip galvanising) but this is generally used for larger parts such as trailers. In this writeup I'm just talking about zinc plating steel via electroplating.

Even though zinc corrodes more slowly than steel it will eventually wear through and after 25 years a lot of the nuts and bolts in the engine bay of my racecar were looking pretty rough. They were still useable but re plating them it gives the car a much more professional look to it. I took the oppourtunity to plate as many fasteners as possible while I had the head off but beware, it's not a quick process. Cleaning and wiring up all of the fasteners takes quite a lot of time and like anything, the better the prep, the better the end result.

The process starts with dipping your nuts/bolts/whatever into a heated caustic soda bath which acts as a grease/oil remover. You need to string the fasteners to thin copper wire so you can retrieve them from the bath.

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Then rinse in water and dip into the muratic acid (hydrochloric acid) bath to remove any zinc plating which is still on the steel. You leave them in here until the fizzing stops which signals the chemical reaction has stopped. This generally only takes about 10 minutes.

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After these two steps you end up with something like this. You can see how I have wired them up in short strings. There is still some zinc remaining - this will be stripped in the next step.

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Your parts then need to be bead blasted to remove any remaining zinc or corrosion. This will also remove any remaining grease or oil but it's not ideal for that job.

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Then it's a quick rinse in water to remove any bead blasting media and then back into the caustic to remove any grease from handling them. Another rinse and then into the galvanic cell. This is where the zinc plating takes place. I'm going to do a shit job of explaining this but basically the solution that the fasteners are submerged in allows zinc ions to travel from the zinc electrodes to the steel parts when an electrical voltage is applied to the system. In the photo you can see the zinc elecrodes attached to the outside of the bath and the steel parts hanging from the bar in the middle. This process takes about half an hour to build up enough zinc on the parts.

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Then another rinse and a VERY quick dip (only a second or so) in the brightener solution which is just nitruc acid. This removes the 'fluff' from the surface of the parts and makes the final product more shiny. Then a rinse and the final step is to dip them in the gold passivate. This is a very important step as it provides another level of protection and it also makes the final product look good. Brightener on the right, passivate on the left:

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A final rinse and then the parts must be left to set overnight. The final result looks awesome and while the process is time consuming it's not very difficult. For the batch I photographed above it took about 3 hours from start to finish.

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Hopefully someone finds this at least midly interesting. Ask questions here if you want!

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Finishing off the manual steer conversion:

So I've already posted pics of the crossmember after it came back from powdercoating and the old and rusty steering rack. The next step was to remove the old crossmember and steering rack (all of the PS lines and pump had already been removed. I supported the engine in a less than ideal manner and dropped the crossmember.

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Followed by the steering column. This must be changed too as the PS racks are taller so the lower segment of the steering column doesn't reach the UJ on the manual steer rack. Luckily I have spares of all this stuff. Column gone:

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Sayonara.

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Stripped the spare rack. Degreased everything. New Rack ends. Bead blasted the UJ and the housing. Painted the steel segement of the housing and the UJ with high temp paint then reassembled it all:

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Did the same with the replacement steering column. Stripped and everything cleaned. Bead blasted the housing and painted it in the silver exhaust paint that I had (I really like that paint). All bearings regreased. And then jammed it all back together.

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Installed the rack with new urathane bushes from Stocks. The D-shaped one is not correct in these kits so I had to cut a section out of it. It still works fine, but it's not ideal. I think AJPS in Aussie has had a new kit made that only he stocks with the correct parts if anyone is keen to do this.

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I reckon it came up pretty good :)

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All bolted in. It was a mission to get this in place with all of the suspension still hanging there. If I was to do it again I'd probably remove the struts or maybe just the sway bar to make life easier. I left the UJ disconnected until I set up the alignment.

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Here's a few more random bits and peices that I did.

Modified radiator support bar back from powdercoating.

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Got a plastic clip for the bonnet bar thingy from Tama Autos.

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Removed unused bracketry. Spotweld drills are awesome.

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Drilled speedholes in the radiator fan mounts and gave them a tidy up. There's plenty more speedholes to come :)

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Aight so back to getting the damn engine running. The last post about the engine was me measuring the valve clearances and figuring out what shims I was going to need. Turns out I'm a moron and that by doing it with the head sitting on a towel the valves had picked up random strands of cotton and thrown all of my measurements off :( So I removed all of the towel bits and did it the right way:

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Finally started getting positive clearances on all valves by juggling around the shims I had. As the valves have been ground quite a lot the shims I need are pretty thin. Managed to get 6 shims from Toyota which cost something stupid like $115 and that was at cost price (the guy at Toyota on Lincoln road is a GC btw). Two shims I needed were unavailable from Toyota so Tony gave them a grind for me. While I was there I picked up the modified Holley fuel pressure regulator. One shim was still not right so I got that ground locally by Glendene Engine Reconditioners. They were nice enough guys but I disapprove of charging $40 to grind one shim when half the time was him scratching his head about how to do it.

Took the car up to Tonys and bolted the head down with the old head gasket to time the cams. I hadn't done this before so having Tony to give me a hand was a huge help! We machined nicks into the bottom pulley to mark the centreline of each cam. By aligning these marks up with TDC and using the dial gauge it is easy to set/check the cam timing without a degree wheel.

Head on:

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Timing it up:

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Checked the piston-valve clearance while we were at it too and it's heaps.

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Finally it was time to bolt it down proper! Dad came and gave me a hand to put the head on and tidy things up. By this stage the pre-trackday panic was starting to set in.

'Water pump' housing on and block/pistons cleaned and ready to go:

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Head on and cams in. Finally!

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The old man bolting the carbs up:

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Modified FPR with gauge to check that it's working correctly:

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Not far away from running now:

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The next night I made this sweet little coolant pipe to fit with my modified water lines from the back of the head. It's a million times better than the previous setup. I really like Supercheaps selection of random radiator and heater hoses, they pretty much always have something that you can make work.

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And installed:

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I slipped the cam belt on to the cam pulleys and gave it a few turns by hand before tightening up the tensioner for the last time. Things just didn't look right at all and after scratching my head for a few minutes I realised what had gone wrong. Tony had accidentally timed the cams the wrong way around! So the inlet was opening before the exhaust. This is due to him being used to working on his Louts motor that has the cams on opposite sides of the head. Legitimate mistake. Luckily I realised before going to start it. So out came the dial gauge to sort things out:

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Finished painting the exhaust. I got the extractors sand blasted as it's impossible to get into the gaps with a wire wheel. I only have a few photos of this part. Before:

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After. Excuse the white balance in this shot. The lights at work make my camera shit itself.

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Extractors painted in high temp 'aluminium' paint by 3M. This is really good paint for something that comes out of a rattle can. The rear section was painted with the same stuff.

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Installed. I really like this shot.

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Set the ignition timing. Managed to ground each plug with some jumper leads and some wire. This way we could crank the motor with no plugs and have them sparking so we could set the timing. I want to make up a plate with some old plugs screwed into it to make this job easier for next time.
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Here's me gazing over it thinking about what I had forgotten before we kicked it in the guts :)
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After deciding we were good go James gave it a crank and we got a whole series of pops and bangs. Some out the exhaust, some out the intake. None where they were supposed to be. FUCK. Turns out the the timing was 360deg out to start with. Whoever set up the CAS when the Link was installed didn't RTFM apparently. Pulled the CAS out and turned it 180deg and jammed it back in the hole. Gave it another crank and this happened! Cheers to Ned for the Vide.



Jeah. I was a happy man. Idled quite nicely when it came up to temp. The carbs were well out of balance from being off the motor though. Called it a night and went home happy as.
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