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beachlander

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Posts posted by beachlander

  1. 14 hours ago, KP_wag said:

    That'd be super cool, matching walnut swirl knob for yer walnut trim dash... 

    Do you finish those on a lathe or do they come out of the mould like that? 

    Yea that's sort of the idea, can do colours etc to match cars or whatever people want. 

    They come out of the mould as either a cylinder or rectangle depending how I make them then shaped on my wood lathe

    • Like 5
  2. On 03/08/2019 at 01:24, ajg193 said:

    I'm not sure how similar a 7M-GE is to a 6M-GE (distributor looks to be on other side of head at least)

    mseriesdist.png.c8e1714b1f58bad163b0b1dd558c54e1.png

    5m/6m is a bit different but i have the manual for it. Have set everything as good as it can be going off the manual so am pretty stumped as to why it wont run now.

    Had it very close to starting but just doesnt want to.

  3. On 30/07/2019 at 16:12, ajg193 said:

    Cam shouldn't be coming onto any valves at tdc compression. I say timing 180 out. 

     

    On 30/07/2019 at 22:13, Mof said:

    #6 should be coming off exhaust and onto intake  (rocking) when #1 is at tdc fyi

    You two were spot on, cams 180 out, idiot.

    Set everything as it should be, and it is so close to running. We have the dizzy just coming onto cyl. 1 at tdc, but it seems like we dont have enough adjustment on the slot to get it where it needs to be. TDC/cam belt is set as good as it can be. Any other suggestions on what it could be? 

    There are a couple of rips on the intake in a few different spots I'll tape up tomorrow. Leads could definitely do with being replaced, but it did run before all this work before, so i would think it would at least fire up.

    • Like 1
  4. Screenshot_20190731_082241.jpg.666f7afc2c9504ebabe83dbb54444d33.jpg

    Screenshot_20190731_082259.thumb.jpg.cc1d4c8773076e13fdd6906fe178922a.jpg

    Swapped the motor and t50 in along with all my suspension from my corolla, PSM coilovers, knuckles etc. 

    Then sent it away to finish off wiring. Screenshot_20190731_082314.thumb.jpg.5ac74affd0e0bd1ceedc644fcae8653e.jpg

    Came back running with just a few things left to do to be able to take it for a drive which I have now done. 

    • Like 4
  5. Yarns: 

     

     

    Had a ke70 a while back, had 4age, t50, t series rear blah blah in it, but the body as well as wiring needed way too much work than I had time/patience/money to deal with. 

    So when this thing came up for sale I grabbed it. Screenshot_20190731_081314.jpg.03b6974b43f66fcec7b41c3b0ce4a11b.jpgScreenshot_20190731_081405.jpg.dac9b94f9292011556fe8db6da169505.jpgScreenshot_20190731_081326.jpg.0d6274eedf0647d8a0f2dbbfd6f46ca3.jpg

    Screenshot_20190731_081336.jpg.7d00f4cf4a6324ff17eca79fb41809dd.jpg

    Screenshot_20190731_081351.jpg.48a1e0d073a0406bf25368cd2c476131.jpg3au, t40 and t series rear. Wof and reg. 

    Plan was to lower it with my stuff from my ke70, put some wheels on then drive it for a bit before swapping in my 4age and t50. 

    But one day driving it it blew its headgasket. I was moving house at the time so it sat in the naughty corner until life was a bit less hectic. 

    Then had some help and pulled motor and box out and 4age went in.

     

    • Like 1
  6. Hello OS, long time no see. 

    So I'm finally trying to get this thing running after ignoring it for far too long. 

    IMG_20190728_174748.thumb.jpg.1e944454a338425c38af6999fc360488.jpg

    So many moons ago I got this thing running after buying it. Ran/idled well but the head was really noisy which ended up being tappets. 

    Pulled the head off (6mge BTW) and replaced tappets, head gasket etc all that good stuff. 

    Assembled head and reinstalled with new cambelt, and it sat for another long break after that, while I spent money on important things such as wheels. 

    Had an attempt or two at getting it running after that but had no real success, would turn over but not fire. 

    Now on the weekend me and @Hachi-ichi had a crack at getting it going. Checked spark, all good. Checked compression, all good, around 145-150 across all 6. Fuel seems to be getting pumped as you can definitely smell it when turning over, as well as plugs being covered in fuel. Also chucked some new gas as the old stuff had been in there for a fair while. 

    Timing seems to be OK. At TDC with dizzy coming onto no.1 cylinder, intake cam is also coming onto no.1.

    But it just won't fire. It had a couple of little pops and bangs but nothing enough to keep it running under its own steam. 

    Have a few more things to check/do such as new fuel filter and some other stuff but was wondering if there is something simple I can check or may have missed, as it seems like it should want to start at this point. 

    Ta

     

    • Like 3
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